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  • IRMC 2010 - Program Guide and Registration Form

    March 11th, 2010
    The 13th annual Iris Rotating Machine Conference program guide and registration form now available. The IRMC will take place June 21th to June 24th in Orlando, FL

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  • ISO 9001:2008

    January 1st, 2010
    Iris Power LP - Now Registered to New Quality Management System Standard

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  • Diagnostic News - Fall 2009

    November 13th, 2009
    The latest edition of this informative newsletter is now available

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  • Turbo-Generator FAILURE PREVENTED
  • Hydro-generator
  • Motor SAVED
  • TIso-Phase Duct: FAILURE PREVENTED

Solve in one move contact Iris Power

Sign

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High PD activity ...

Problem

Solve in one move contact Iris Power

... lead to uncovering a critical problem - the incorrectly installed wedges

CLOSE

PROBLEMS IN HYDROGEN COOLED GENERATOR REVEALED

Company: Midwest US Utility
Ratings: 173 MW, 18 kV, Hydrogen Cooled Turbine Generator, 3 years in operation
Manufacturer: Confidential
Related Info: 25 years old
PD Sensors: Two bus couplers per phase
Case Study Details:"... With the high H2 pressure (30-35 psig) the [PD] levels were expected to be very low but instead were very high after only a year of operation. We initially expected to find problems with the couplers as we did not believe the results..."

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216 CONFIRMED PROBLEMS WERE DETECTED WITH ON-LINE PD TEST

  • Contamination: 10
  • Vibration: 54
  • Design/Manufacturing: 127
  • Operation/Maintenance: 12
  • Non-Generator: 13
  • Total: 216

Click here to read more

Sign

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High PD activity (slot discharge)...

Problem

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...was a foresign of an upcoming failure

CLOSE

HYDRO GENERATOR WITH VERY HIGH PD FAILED IN-SERVICE

Company: Western Canadian Utility
Ratings: 184 MVA, 13.8 kV, Air Cooled Hydro Generator
Manufacturer: Confidential
Related Info: 25 years old
PD Sensors: Four PDA Couplers per phase
Case Study Details: The PD data for this unit has been trended for over ten years. In 1995, semi-conducting paint and CRTV were injected into selected bars ...

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216 CONFIRMED PROBLEMS WERE DETECTED WITH ON-LINE PD TEST

  • Contamination: 10
  • Vibration: 54
  • Design/Manufacturing: 127
  • Operation/Maintenance: 12
  • Non-Generator: 13
  • Total: 216

Click here to read more

Sign

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Intelligent on-line signature analysis...

Problem

Solve in one move contact Iris Power

...revealed broken rotor bars

CLOSE

BROKEN ROTOR BARS IN CONDENSATE PUMP MOTOR DETECTED

Company: A large utility in the US northeast
Ratings: 3000hp, 6.6kV 1785rpm Motor
Manufacturer: Confidential
Case Study Details: The suspicion arose from a constant hum during motor operation and abnormal vibration levels during start-up and running. The plant vibration monitoring system did not have the ability to zoom...

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Sign

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High level system PD noise...

Problem

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...uncovered a well-developed tracking

CLOSE

HEAVILY TRACKED BUSHING DETECTED

Company: Italian utility
Ratings: 390 MW, 20kV, Hydrogen Cooled Turbine Generator
Manufacturer: Confidential
Related Info: Installed in 1970
PD Sensors: Two Bus Couplers per phase
Case Study Details: During a partial discharge measurement using the TGA-B portable instrument, high levels of PD activity (over 3000mV position, well above the highest range, see Figure 1) were detected on the C phase outside...

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216 CONFIRMED PROBLEMS WERE DETECTED WITH ON-LINE PD TEST

  • Contamination: 10
  • Vibration: 54
  • Design/Manufacturing: 127
  • Operation/Maintenance: 12
  • Non-Generator: 13
  • Total: 216

Click here to read more

Sign

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Reading Instability...

Problem

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...uncovered internal bad connection on a new transformer

CLOSE

BAD INTERNAL CONNECTION TO BUSHINGS UNCOVERED

Company: US North-West utility
Ratings: 45 MVA power transformer
Manufacturer: Confidential

A customer was commissioning a new 45 MVA power transformer delivered by an overseas manufacturer. During the test, ADWEL's Digital Winding Resistance ReporteR, DWR-10, was consistently issuing a warning of current interruptions, and did not complete the test. Another DWR-10 instrument was used with similar outcome. All other standard measurements, including TTR, Tan-Delta and insulation resistance indicated acceptable resistance value.

Nevertheless, the customer drained the oil and inspected the transformer to detect that the windings on all 3 phases were not properly secured to the bushings. Had the transformer been energized, a catastrophic failure could have occurred.

Click here to learn more on DWR-10

Technical Papers

Select Topic:

File Name
EIC 09 - Stator Winding Hipot Testing.pdf
Hydro 05 - Important considerations for specifying new hydrogen SW.pdf
HydroReview 93 - Using diagnostic technology for identyfying generator winding maintenance needs.pdf
Partial Discharge Testing A Progress Report - IRMC 2009.pdf
recent problems experienced with motor and generator windings - IEEE PPIC - 2009-06 sep 2009.pdf

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